turkey point power reactor down, internal problems versus control problems

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+------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36618 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: TURKEY POINT REGION: 2 |NOTIFICATION DATE: 01/24/2000| | UNIT: [] [4] [] STATE: FL |NOTIFICATION TIME: 12:50[EST]| | RXTYPE: [3] W-3-LP,[4] W-3-LP |EVENT DATE: 01/24/2000| +------------------------------------------------+EVENT TIME: 11:42[EST]| | NRC NOTIFIED BY: DAVE MORRIS |LAST UPDATE DATE: 01/24/2000| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |KERRY LANDIS R2 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |4 M/R Y 95 Power Operation |0 Hot Standby | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MANUAL REACTOR TRIP DUE TO FEEDWATER OSCILLATIONS | | | | The licensee had reduced power to 95% to examine the '4A' steam generator | | feedwater regulating valve due to feedwater oscillations. A preliminary | | determination of valve internal problems versus control problems was made. | | The licensee was ready to continue the down power to shutdown to repair the | | feedwater regulating valve, when a manual trip became necessary due to the | | feedwater oscillations on '4A' steam generator. | | | | All systems functioned as designed, all rods fully inserted, no secondary | | safety valves lifted, and the plant is stable in Mode 3. Heat removal is | | via the atmospheric steam dumps, normal procedure with no tube leaks, and | | feedwater is via the standby feedwater system. The plant will remain shut | | down until repairs to the feedwater regulating valve are complete. | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+

-- boop (leafyspurge@hotmail.com), January 25, 2000

Answers

Boop, why do you clog the forum with clearly irrelevant postings

-- Mr. Sane (hhh@home.com), January 25, 2000.

Mr. Sane

Did you ever have a pet puppy as a child?

-- justwondering (justwondering@trollsareunsound.com), January 25, 2000.


Thanks boop, ingnore the flatulence

TURKEY POINT 4 01/24/00
Hot Standby
MANUAL REACTOR TRIP DUE TO FEEDWATER OSCILLATIONS.

-- spider (spider0@usa.net), January 25, 2000.


When Mr. Sane was born there was a little turd and a baby came out...The baby died!

~~~~~~~~~~~~~~~~~~~~~~~~~~Shakey~~~~~~~~~~~~~~~~~~

-- Shakey (in_a_bunker@forty.feet), January 25, 2000.


GRAND GULF 1 14%
REDUCED REACTOR POWER TO TAKE
MAIN GENERATOR OFF LINE DUE TO A
HOT SPOT ON THEIR MAIN TRANSFORMER.

-- spider (spider0@usa.net), January 25, 2000.


NO NUKES is GOOD NUKES

-- liberator (feeding@the trough.com), January 25, 2000.

Boop & Spider: Thanks for the info.

Insane: Go Jump in the lake (preferably one in Siberia).

-- TrollStomper (DoomersUnited@TB2000.Net), January 25, 2000.


I know Turkey Point is in Florida, but where?

-- Mara (MaraWayne@aol.com), January 25, 2000.

East of Homestead, south of Miami, and north of Key Largo.

-- Postman (ringstwice@lw.ays), January 25, 2000.

Mara, It is about 8 miles South of my house. When I go sailing at Black Point Marina I can see it. If anyone hears anything else, I would appreciate if you let me know. Makes me a little nervous.

-- JoseMiami (caris@prodigy.net), January 25, 2000.


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